Summary - April
After the March competition, we decided that we needed to narrow the frame, add a sensor to detect the protons, and develop a new stopping/attachment appendage. Narrowing the frame was serious work because we had to partially disassemble the robot. The sensor was easy to attach, but it required our programmer to add additional code to our program. The appendages were a problem; we discussed many ideas and prototyped two. The first one didn't work; we're hoping the second works as planned.